Thursday, July 21, 2011

In retrospect the post I wrote Wednesday night\Thursday morning was a ry, technical report written in exhaustion and under the influence of a few celebratory drinks.

It is probably time to fill in the rest of the story.

There was of course a large amount of initial nervousness on my part, let alone my wife. Vivian only had gave me conditional permission to execute the first flight if Tom was there flying chase. In turn Tom made me promise not to mar his perfect history of first flights without an incidents.

The real pre-flight inspection was done on the 19th to make sure nothing was missed due to nervousness. I had practiced some of the first flight in the 150 on Sunday with Tom riding as an instructor. We also practiced HAPL.

On the 19th after the DAR visit, my own inspection and putting all the hatches back together I wanted to do a run up. This way I knew I would have enough battery to start for the first flight and maybe catch a few issues. The weather was extremely good and the airport was empty so I did some taxi testing on 34. The first pass was just to see how far I had to go for the airspeed indicator to come alive. Then I went as far as to rotate the nose. At this point the rudder still did not seem THAT stiff.

Flash forward to the 20th. I flew up to AWO from BFI for the test flight. Flying immediately before hand was probably the most calming thing I could have done. It got me in a flying mind set and also let me know the real conditions aloft. There was no guessing if the air was smooth or not.

Going over emergency procedures, bailout procedures, ect was a little stressful. The idea that that I may have to trust a parachute packed by someone else just seemed wrong. If my day was going that bad, then how much worse could it get, right?

We removed everything from the plane and vacuumed it out once more. Only stuff riveted, bolted or screwed down remained except for the bottom section of my seat cushion. I only had a three printed pages ( two pages of checklists\procedures and the test card ) and a voice recorder taped down and jacked into the intercom. The tape of course ran out during the flight.

The run up seemed to take forever. And it really did. You can’t fly the Rotax until the oil gets to 120F. That meant some idling to get the engine warm enough.

For this flight there was a clear division of labor. Tom was going to handle the radios from the Cessna. I just needed to stay on frequency to communicate with him. He was to keep traffic clear and advised.

With the run up done and the pattern clear there was nothing left to do but to just get the flight over with. This was the peak of my nervousness.

I had this expectation that as I advanced the throttle every single bolts and rivet would flash through my mind. That did not happen, instead I actually relaxed a bit and tried to enjoy the ride. Concentrate on the signals the engine is giving you, keep down the middle and wait for the bird to leap.

At this point the closest aviation experience I’ve had was my first solo… that combination of a familiar plane climbing unfamiliarly fast paired with “now I have to land this by myself”. By 1000’ that was out of my mind. At 3000’ I was getting a little bored of turning left and climbing.

Then another strange thing happened. Tom was trying really hard to stay out of view and the 701 was doing a really good job of running away from my poor 150. Looking down and seeing my 150 more than 1000’ feet below trying really hard to keep up was very strange. Then during some of the turns I caught sight of it again through the big door windows, but much closer. It was something like watching the race scene from “Iron Eagle”. There was this little white plane with a red stripe turning so beautifully against the mountains and clouds. The 701 also slows down MUCH faster than a 150 and Tom went darting past me whenever I cut the throttle back.

The turns to the left and to the right were no big deal. I really had to restrain myself from going more than standard rate.

The 701 does not have a centering spring in the rudder or pedals. In addition it uses an all flying rudder with wetted area ahead of the hinge. If you push left rudder, it stays left rudder until you push it back. This is hard to remember. You also really need to lead your turns with rudder first, which is also hard to remember to do after so many years in a 150 where generally you use rudder and ailerons at the same time. Every once and I while I would see I was un-coordinated and push the rudder causing a bit of a skid.

When coordinated the 701 turns VERY tight. It is reasonable to fly the pattern only ¼ mile out, do a standard rate turn and expect to lined up for final. Hitting the rudder to get coordinated would skid you into coordination and really remind you of this.

The practice approaches were really nothing special and I have nothing more to say about them.

Landing was the ugly part. I knew I had tons of runway to allow myself to settle in. I knew I needed to carry power into the landing. I knew I had to hold the flare until last minute. These things blanked on me until I had already started to flare and felt that sinking feeling that makes every pilot think they will have to bend the gear back into shape. So of course I added power, but a little too much and got back up to where I started. Letting power out that time gave me a better sink rate but it was still a firm landing. Then I had the steering\rudder stiffness to contend with.

My thought is that the landing may have loaded the bungee strut putting more pressure on the front contact area, making the stiffness worse. Maybe stick back pressure would have helped.

All said and done the first flight took about 25 minutes and it seemed like 25 minutes. I didn't not any sense of time dilation or contraction. I remembered to breath and did some instrument scans. I was only tense for a few moments, most of which occured during the landing.

Thanks again to everyone who has helped, voiced support, stopped by my hangar, ect.
N701GV had its first flight around 5:30PM on Wednesday 7/20.

I flew my Cessna 150 up from BFI to to AWO and met Tom Staggs. He then took my C150 and flew chase.

The engine in N701GV is a 912ULS producing 100HP at 5800RPM. The prop is a three bladed Warp Drive High Power pitched to 11.5 degrees. Static run up RPM is 5500. It currently DOES NOT have strut fairings or tail VGs. Empty weight is 626lbs.

Everything went as well as could be hoped. John Adams will get his helmet and parachute back un-used. There are a few items that I will fix before the next flight.

The objectives of the test were met and all steps of the first flight's test plan were completed.

Overall N701GV behaved very well and displayed no bad in-flight control characteristics. The flight controls felt balanced and no wings felt "heavy". The rudders were stiff in flight making fine corrections hard,

The flight test was pretty simple. I slowly advance to full throttle and then let the plane jump off the run way. At about 300' above ground I offset with the runway under my left. At 1000' above ground the plane was climbing so fast there was still runway ahead.

I then started a gentle left, climbing turn to keep in a cone of safety that would allow me to glide back to the runway in case of engine failure leveling off at 3000'

With that done I then evaluated basic left and right turns up to 15 degrees of bank and a descent. The descent proceeded into a simulated approach and a go-around.

This was repeated again descending down to 1000' above ground. One more practice approach was made to only 50' above the runway climbing back to 1200'.

Finally a full landing was made. It was not my best landing. I started the flare too high and came in a little hard to the left of center and barely was able to overcome the rudder friction to stay on the runway. Control friction was probably the largest factor, but loading of the nose strut may have also played a role.

I pulled the cowling and all inspection plates\hatches. No leaks were found and all bolts remained tight with Torque-Seal markings intact.

Several issues were found that need to be resolved before the next flight.

Bug#1 - The control tension for the rudders made for a stiff control system. This made fine tuned flight corrections hard and presented a challenge after touchdown for remaining in the center of the runway.
Bug#2 - The Garmin 496 GPS draws some amount of electricity from the main battery all the time. This keeps the GPS internal backup battery charged, but also reduces the available cranking amperage for starting. I will install a disconnect switch to cut the charging mechanism to allow for long term storage.
Bug#3 - The passenger side door displayed puckering during high power settings. An additional aft locking pin slaved to the main door latch will be installed.

Tom was kind enough to grab a pic while I was flying. I also took a portrait of N701GV yesterday after the DAR visit.

The flight back to BFI was pretty boring.

Tuesday, July 19, 2011

The friendly regional DAR stopped by on Tuesday morning.

Overall it was a pretty easy experience. A fellow 701 builder, Curt Thompson, was there to observe the process and see what the DAR would look for in a 701. He also wanted to avoid any mistakes I had made.

The appointment was for 10AM and the plane was mostly already opened up, IE all access hatches, inspection plates, ect. Only the top cowling had not yet been removed.

I had a table setup with all the paperwork in order.

The basic safety inspection started at the nose, moved back to the cabin, to the pilot side wing, control access hatch, the empennage, passenger wing and finally back in the cabin.

Generally he checked that cables and wires were properly secured, gas and electrical separates, bolts were tight and proper length, ect. He also checked control continuity and correctness for the engine, flaperons, elevator, elevator trim and rudder.

Placcards were also checked.

As always what you worry the most about never receives attention. I spent a long time worrying about details like the registration numbering. The FAA has very strict guidelines concerning the spacing of the numbers. He just looked up and made sure it was there.

Then there were things that I was sure he would think were wrong, but are by plans. The prime example are the control surface hinge bolts. The Zenith design uses a bearing surface squished between two bolts, no cotter pin. I have spent so much time explaining that the bolts are never under rotation that I had bookmarked the plans page. He had just done a 750 so it never came up although he did check the bolts.

Of course he found some minor issues, but nothing that would block an airworthiness certificate. I was able to address his punch list within a few hours.

After a break and a lunch I reinstalled all inspection plates and the cowling. That was then followed by a complete walk through taken from my POH for both pre-flight and 1 month inspection routines.

I had not touched the plane for a few weeks so the combination of running electrical for the inspection and the Garmin GPS trickling a small charge gave me a hard start.

Runup went well and I took my time doing it to charge the battery. I taxied the plane onto AWO 34 and performed a few taxi tests. Everything went smoothly, but I really didn’t do much. Airspeed comes alive on the Dynon at ~25MPH just as the nose wheel gets light.

I decided to trim the wing root covering some more to help reveal the forward wing-root cover bolts. I also found a few bolts without torque-seal.

Wednesday, July 06, 2011

Finished major construction, ready for the DAR.

Added trim to wing root skins. Secured strobe\nav wires in baggage compartment.

Added tangs to rudder cables to effectively lengthen them. Neutralized rudder and brake pedals. Safety wire and secured rudder turnbuckles. Added cotter pins to all steering assemblies.

Added adele clamps to secure brake lines.

Finished securing wires in hatch.

Fitted scat tubing to oil cooler and re-bonded NACA duct.

Chased down a squeak in the elevator.

Final check for all bolts, pins, wire.

Found prop serial number ( without having to disassemble! )

Did static runup to verify full power and prop pitch. 5500RPM at 11.5 degrees pitch.

Wrote "Fuel On" \ "Fuel Off" placards on floor since stickers would not stick.

Performed fuel flow test at nose high attitude.

Punch List:
FINISH PROCEDURES\MANUAL
Emergency flight refresher ( simulated engine out, ect )

Trim passenger side door fiberglass, add rubber trim.
Fabricate, install streamlined strut covers. ( post first-flight )
VGs on elevator ( after initial test flights )

Sunday, July 03, 2011

Found some more nut plates and added them to the trim servo access hatch.

Made a fork and then riveted in a small bracket to help keep the fire extinguisher from coming loose.

Drilled and deburred wing root covers to final A4 size.

Neutralized and set flaperon controls. Re-set aileron bump stops. Setting the ailerons is tricky, made worse when alone. First it is hard to determine the true up-right neutral position of the stick. Then you have to verify the lower torque tube bellcrank is in alignment ( not that much could be done about it now... ).

Finally it is a long slow process of measuring reference lines from the wing for gap distance. One trick I realized was to measure the angle between the rivet line for the push rod covers against the extrusion the connects the flaperon to the pushrod.

Luckily I had left the inboard pushrods coming from the torque tube long. This gave me more choices on setting the amount of reflex or deployment for a flaps up position.

The pushrods and jam-nuts are not flight ready.

The aileron bump stops are not the best designed items. Their placement is some what arbitrary and can be hard to align properly.

Using the darkness I verified the landing lights are aimed correctly.

On Tuesday the final securing of wires will be done. The steering push-rods will also get set.

Punch List:
FINISH PROCEDURES\MANUAL
Shorten steering pushrods, install plates to lengthen rudder cable.
Fuel flow test
Final securing of wires aft of seats in luggage
More cotter pins & safety wire ( flaperon pushrods & steering pushrods )
Safety wire turnbuckles on rudder cables.

Install wing root fairings ( post inspection )

fabricate, install streamlined strut covers. ( post first-flight )
VGs on elevator ( after initial test flights )

Saturday, July 02, 2011

Fabricated wire supports in access hatch. Created addition support for fire extinguisher.

Debugged transponder issue. I suspect it may have been caused by the GPS input on pin 2. Setting the Dynon to 29.92 matched the pressure altitude shown on the Garmin 327. Turning off the Dynon blanked the pressure altitude reading.

The manual indicates ( in very small print ) that NMEA inputs are not supported from the 396\496. Therefore I pulled the #2 pin to remove the input. This may have been a grounding issue caused by the GPS input or a software issue caused by the transponder attempting to decode bad input.

Found that taxing had loosened a bolt holding the passenger side nav light. Drilled out wing tip and tightened. Tips held by screws would be best, but may be impossible.

Punch List:
FINISH PROCEDURES\MANUAL
nuetralize aileron rods & control
Shorten steering pushrods, instal plates to lengthen rudder cable.
Final securing of wires aft of seats in luggage
More cotter pins & safety wire ( flaperon pushrods & steering pushrods )
Safety wire turnbuckles on rudder cables.

Install wing root fairings ( post inspection )

fabricate, install streamlined strut covers. ( post first-flight )
VGs on elevator ( after initial test flights )

Friday, July 01, 2011

Made a first attempt at transponder inspection. Bits were being adding on the discrete code while in the plane, but not on a bench. Not cause has been identified yet.

Added reinforcements to the radio stack. Tightened and flight readied all nut plates related to the radio stack.

Adjusted aim of landing lights.

Installed nutplates and cover for elevator trim motor.

Punch List:
Fabricate wire bundle supports for rear cargo area.
Have transponder tested by avionics shop
FINISH PROCEDURES\MANUAL
VGs on elevator
nuetralize aileron rods & control
Shorten steering pushrods, instal plates to lengthen rudder cable.
Final securing of wires aft of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
fabricate, install streamlined strut covers. ( post first-flight )

Monday, June 27, 2011

Had a project visit and identified a few more minor changes.

Lost the elevator trim servo cover ( held on by clecos ) during a runup test.

Torqued more bolts to final, riveted flaperon covers into place. Touched up primer on a few steel parts.

Fixed tachometer reading on Dynon. Tied down more wire bundles.

Punch List:
Fabricate wire bundle supports for rear cargo area.
Fabricate new elevator servo cover.
Have transponder tested by avionics shop
FINISH PROCEDURES\MANUAL
VGs on elevator
nuetralize aileron rods & control
Shorten steering pushrods, instal plates to lengthen rudder cable.
Final securing of wires aft of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
fabricate, install streamlined strut covers. ( post first-flight )

Sunday, June 26, 2011

Tensioned elevator. Re-adjusted slack bungee, added nylon blocks where elevator cables could rub. Safety wired elevator turnbuckles. Removed elevator and adjusted bolts, installed & castelated elevator bolts.

Finalized rudder bolts.

Bolted battery into position.

Installed dataplate.

Greased all bushings, control bolts.

Aimed landing lights.

Punch List:
Tighten passenger door ( opened during run-up )
Have transponder tested by avionics shop
FINISH PROCEDURES\MANUAL
VGs on elevator
nuetralize aileron rods & control
Shorten steering pushrods, instal plates to lengthen rudder cable.
Final securing of wires after of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
fabricate, install streamlined strut covers. ( post first-flight )
Correct tach reading on Dynon, reconnect hobbs meter.

Saturday, June 18, 2011


Re-weighed the plane.
Nose: 162lb, arm=670mm
Left main: 232, arm= = 690mm
Right main: 232, arm = 670mm

Added RTV seal & trim around fuel neck filler & wing skin. Tightened a few more bolts & added cotter pins to all but two steering & rudder nuts. Added fuel type markings.

Tightened bolts between steering push rods and nose strut along with jam nuts.

Found fuel senders were "double grounded" and pins were crossed. Fixed fuel sender wiring. Flushed fuel system and calibrated Dynon fuel sensors.

Bled brake lines.

Charged battery.

Started engine from fuel in wing tanks.

Taxied under own power across the airport. Started break-in procedure for Matco brakes. Verified steering and brakes.

Punch List:
FINISH PROCEDURES\MANUAL
Final placement of battery
Install EAB plaque
VGs on elevator
nuetralize aileron rods & control
Final securing of wires after of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
fabricate, install streamlined strut covers. ( post first-flight )
Install steering boots
Install nylon strip in service hatch to protect against elevator cable rub
Remove elevator & grind down clearance of center hinge.
Correct tach reading on Dynon, reconnect hobbs meter.
Aim, secure landing lights

Wednesday, June 15, 2011

Did a bolt\torque check. Identified all untighted and overtorqued bolts. Replaced all severly overtorque bolts. 95% of all exterior bolts now flight ready. Almost all cotter pins installed, all others marked. Removed the dorsal fin. trimmed the top fuselage skin at the elevator cable exit and moved the reinforcement bulkhead forward to account for the bungee tension.

Ordered some nylon to mitigate rubbing of the elevator cable on the baggage compartment.

Gave the EAB plaque to the engraver. Worked on procedures and manual.

Took an initial weight measurement of 621 pounds.

Punch List:
FINISH PROCEDURES\MANUAL
W&B
Final placement of battery ( pending W&B )
Install EAB plaque
Fuel Filler Marking for 10G 92MoGas\100LL w/TCP
Post registration in cabin
bleed brake lines
VGs on elevator
nuetralize aileron rods & control
Fuel tank calibration
Final securing of wires after of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
Torque seal push rod jam nuts.
fabricate, install streamlined strut covers. ( post first-flight )
Install steering boots
Install nylon strip in service hatch to protect against elevator cable rub

Wednesday, June 08, 2011



Finished transition training. Adjusted elevator tension bungee. Trimmed wingroot covers, ready for rivetting once fuel system is fully tested. Installed fire extinguisher. Added extra nutplates for cowling. Epoxied NACA inlet adapter for oilcooler. Fitted washers for bellcranks. Created steering boots.

Trimmed, primed and installed dorsal fins. Bunch of small stuff.

Punch List:
FINISH PROCEDURES\MANUAL
W&B
Final placement of battery ( pending W&B )
Engrave & install EAB plaque
Fuel Filler Marking for 10G 92MoGas\100LL w/TCP
Post registration in cabin
bleed brake lines
VGs on elevator
nuetralize aileron rods & control
Fuel tank calibration
Final securing of wires after of seats in luggage
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
Torque seal push rod jam nuts.
fabricate, install streamlined strut covers. ( post first-flight )
Install steering boots
Install nylon strip in service hatch to protect against elevator cable rub

Sunday, May 22, 2011

Fabricated a replacement bellcrank spacer and installed it. Fabricated replacement jury strut. Disassembled flaperons and primed them. Riveted flaperon root pins. Greased flaperon bearings and reinstalled flaperons. Cleaned up wing root skins and ready them for final trim. Installed a stiffener underneath the dashboard trim, partially pulled the panel lights and re-installed them so to not tension the dashboard again.

Punch List:

Got a ton of stuff done this weekend:

Fabricated and installed the oil door, installed a few cotter pins, removed the elevator trim and modified the hinge to accept safety wire, installed the elevator tensioning bungee, re-installed the doors, fabricated access panels into the seat pans, installed the access panels and re-installed the seat pans.

Punch List:
FINISH TRANSITION TRAINING
FINISH PROCEDURES\MANUAL
install wingroot covers.
W&B
Final placement of battery ( pending W&B )
Engrave & install EAB plaque
Fuel Filler Marking for 10G 92MoGas\100LL w/TCP
Post registration in cabin
mark "EXPERIMENTAL" on entry way
bleed brake lines
VGs on elevator
nuetralize aileron rods & control
Fuel tank calibration
Final securing of wires after of seats in luggage
install first-aid kit and fire extinguisher
Washers for aileron bellcranks
Nose gear pushrod boots
Install dorsal fin
Two additional cowl fasteners
More cotter pins & safety wire
Safety wire turnbuckles in "double wrap" style
Torque seal push rod jam nuts.
fabricate, install streamlined strut covers. ( post first-flight )
finish priming bare surfaces.

Sunday, May 15, 2011

Got a ton of stuff done this weekend:

Fabricated and installed the oil door, installed a few cotter pins, removed the elevator trim and modified the hinge to accept safety wire, installed the elevator tensioning bungee, re-installed the doors, fabricated access panels into the seat pans, installed the access panels and re-installed the seat pans.

Punch List:
FINISH TRANSITION TRAINING
FINISH PROCEDURES\MANUAL
install wingroot covers.
W&B
Final placement of battery ( pending W&B )
Engrave & install EAB plaque
bleed brake lines
VGs on elevator
Adjust control tension
nuetralize aileron rods & control
N-Number on panel
Fuel tank calibration
Re-fab spacer on passenger side aileron bellcrank
Re-fab diagonal pass side jury strut
Final securing of wires after of seats in luggage
install first-aid kit and fire extinguisher
Washers for aileron bellcranks
Grease on bellcranks
Nose gear pushrod boots
Install dorsal fin
Two additional cowl fasteners
More cotter pins & safety wire
fabricate, install streamlined strut covers.
finish priming bare surfaces.

Tuesday, March 01, 2011

The weekend was somewhat frozen and short on time at the hangar. The aileron stops are installed. I adjusted the flaperon and aileron pushrods to what may be a nuetral position, testing will tell for sure.

I fabricated the flaperon bungee rention system, but am having problems reaching underneath the seat to install the bungee cord.

The new landing gear leaf is in. Hopefully it and the brake lines can be installed in a few weeks. Following that only the jury struts and dorsal fin will remain for installation.

Monday, February 21, 2011



Latest work:

Skylight and windshield all installed and unwrapped.
Interior painted and ready. Only a few more wires need to be secured in the cabin
Controls re-installed with continuity restored. All lingering clearence issues fixed.
Rudder pulleys and flaperon mixed riveted down
Sealant & RTV installed to prevent leaks

Punch List:
W&B
Final placement of battery ( pending W&B )
Engrave & install EAB plaque
Install new Grove gear
Brake lines
Cotter pin on bungee pin & outer sleave to tighten
Fabricate top bungee retaining pin
Drill cotter pin holes for elevator bellcrank, elevator retainer and flaperons
VGs on elevator
Adjust control tension
N-Number on rudder
N-Number on panel
Fuel tank calibration
Washers for aileron bellcranks
Tensioning bungee for elevator
Flap handle bungee
Spinner final install
Grease on bellcranks
Yellow plug succured on engine spray rail
Nose gear pushrod boots
Path door fiberglass
Install dorsal fin
Oil access door
Two additional cowl fasteners

Monday, January 31, 2011



Starting to apply finishing touches.

I uninstalled all the controls, cleaned and painted them. I cleaned out the cabin, vacuumed it and blew it out with air. Once that was done painting started.

The control stick was ground down for extra clearance .

Sound deadening material will be cut to be floor mats.

Saturday, January 29, 2011



Secured the dashboard and panel. Gave the panel good labels. Sealed the weather trim to the windshield and did weather sealing for the skylight. The skylight is riveted in a final install.

Monday, January 17, 2011


Another weekend of finishing work.

Preperations are being made to button the dashboard onto the panel. I filled all the grommet holes in the firewall with high-temp RTV. I also fabricated patches to cover the holes where the Zenith style throttle linkages passed through the firewall. They also received RTV along with rivets.

A new panel light was installed to replace the one that was damaged while in storage.

Label the panel
Patch fiberglass on doors
Final windshield install + sealing
Seal sunroof
Order & install steering boots
Adjust control tensions
Check all cotter pins, saftey wire, bolts
Install elevator VGs
Install dorsal fin
Final upholstrey install
Install oil door.
Replace gear with Grove brakeline drilled gear ( ordered )
Run brake lines
Install jury struts
EAB plaque
Adjust nose strut
Final battery box secure
More transition training
Insurance
Smooth any remaining rough edges.

Thursday, January 13, 2011



The engine started without problem.

New punchlist:

Patch fiberglass on doors
Final windshield install + sealing
Seal sunroof
Order & install steering boots
Adjust control tensions
Check all cotter pins, saftey wire, bolts
Install elevator VGs
Install dorsal fin
Final upholstrey install
Install oil door.
Replace gear with Grove brakeline drilled gear
Replace landing gear pads
Run brake lines
Install jury struts
EAB plaque
Adjust nose strut
Install control boots for steering rods.

Thursday, November 04, 2010

The new punchlist:

Fuel lines run from wings to gascolator
Fuel filter
Run line for AOA into wing
Install ammeter shunt
move solenoid location
Install final wires to bus
Wire batter & alternator together
Install split throttle
Install choke

Patch fiberglass on doors
Order Garmin 496
Create wire access port on dashboard
Final windshield instal + sealing
Seal sunroof
Order & install steering boots
Final instal on position light wiring
Adjust control tensions
Final wire secure in hatch
Check all cotter pins, saftey wire, bolts
Install elevator VGs
Install dorsal fin
Final upholstrey install
Install oil door.
Replace gear with Grove brakeline drilled gear
Replace landing gear pads
RTV the FWF firesleeving
Run brake lines
Install jury struts
EAB plaque
Instal static port

Monday, August 23, 2010



The engine is almost ready to go. Below is the "punch list" that I could come up with. More is likely to be added

  • Install battery
  • RTV the FWF firesleeving
  • Replace pads on main gear leaf
  • Replace main gear leaf with Grove replacement
  • Run brake lines
  • Elevator cables
  • Hang flaperons, connect to push rods
  • Wire amp shunt
  • CHT calibration, install
  • Upholstery for interior
  • Install elevator trim motor
  • Replace temp tie down stations with adele clamps in aft fuselage
  • Replace aileron bellcranks
  • Clean off sharpie markings
  • Finish re-run of strobe, nav wires & map lights
  • Run fuel lines from wings to gascolator
  • Install jury struts
  • Prime V-Frame
  • Cargo net
  • EAB plaque
  • Steering rod boots
  • Install fuel filter
  • Fix bad fiberglass trim on passenger door.
  • Run AOA line
  • Install static port
  • Install Pitot/AOA tube
  • Replace bad rivets

Monday, March 08, 2010

Thanks to a team of really great friends, the project is now in at an airport.

I have worked up a punch list of the stuff that needs to be done before the first flight, but engine start should be before the end of March.


  • Finalize access hatch

  • Replace bad rivets

  • Finish securing wires

  • Buy Oddessy battery

  • Run battery cables

  • Ammeter shunt

  • Battery charging

  • Starter

  • Mags

  • safety wire

  • cotter pins

  • More AN3-4As

  • Brake lines/line clips

  • Rudder pedals

  • Attach wings

  • Elevator bungee

  • Elevator cables

  • Rudder cables

  • Paint

  • Seal windshield, sunroof

  • Attach slats

  • Attach flaperons

  • Slat push rod covers

  • Trim doors

  • Fill door tubes

  • Upholstry

  • Sound deading material

  • Fuel lines/firesleeving

  • Carb heat kit

  • Strobe/position final run

  • Pitot/AOA tube

  • Rivet wingtips

  • Wing root covers

  • Vinyl decals

  • Data plate

  • Install elevator trim motor to elevator

Sunday, February 28, 2010



I spent a day fixing the horizontal stabilizer. About a year ago a test fitting revealed that the forward mount points for 10mm to far inboard on each side.

The entire skin was unzipped. With some careful measuring and luck, I was able to use two existing holes on each side that were 10mm outboard. Many of the bracket holes to the spar became elongated so I enlarged them to A6. The old holes were filled in with A5 rivets.

I took the electrical system apart... again ( fourth time? ) and used an aviation grade spiral wrap conduit to add order to the wires. I then added a piece of L-Angle near that crossed from the pilot side to the passenger side attaching to the bus mount I had fabricated earlier. This was done forward and rear. These provide a very nice spot to secure the bundles against.

Sunday, January 24, 2010



The panel is being put back together on the bench. I found a few small problems with the wiring and am fixing them while it is easy.

I used a rubberizing paint on the panel to make it scratch resistant, insulated and glare resistant. So far I am happy with the results.

Using "The GIMP" I have been creating a series of concepts and variations of the paint job. Taking photos of the project the concepts have been laid over to help judge how it will look on the 3D plane.

Thursday, January 21, 2010



I finally got around to finishing my ( new style ) cowling.

The current version of the manual is incomplete and incorrect. I used a combination of advise from Roger at Zenith, the forum and the HBH video.

Here is how I did it:

1) Fit the top and bottom halves together, sliding the top half into the lip. I then made sure the the seam between the top half and the recessed lip of the bottom half was OK.
2) Clamped and taped it together.
3) Determined the center of the top half of the cowl and the center of the airplane. I then extended forwarrd the rivet lines on the side of the fuselage to use as reference for getting it even.
4) I then determined the angle of the cowl and got it centered and even. I used the seam lines on the cowl in conjection with some rivet lines on the fuselage to get it even and centered.
5) Once I had that I then marked where I neeeded to trip the cowling to clear the gear leg and windshield. I only trimmed the gear leg hole a bit, the molding supplied a large amount of clearence. I trimmed a small a amount of the top cowling to clear the windshield and sealing.
6) Once I had the the cowl trimmed I then drilled and clecoed the front four holes to join the top and bottom halves. I determined my safe area of the fuselage flange taped the cowling into place and drilled the cowling into the fuselage flange. I made the holes A4 sized.
7) I removed the cowling. and clecoed the nutplates onto the bottom cowl for the forward holes. I put the nutplates on the "wrong" side so the barrel was pointing away from the plane.
8) I got each plate parallel with the lip of the cowl and drilled one hole with an A3 bit and clecoed. I then drilled the remaining hole.
9) Removed all the nutplates and drilled the center hole out to AN3.
10) Cleaned & deburred the holes
11) I applied a slight countersink to the A3 holes that hold the nutplate using a hand reamer. Use A3 blind rivets to secure the nutplates. Do not drill out the holes on the nutplates.
12) I drilled out the holes on the top cowling to AN5
13) Using a flat riveter head I riveted the nutplates to the inside lip of the bottom half so the barrel pointed into the airplane.
14) I clecoed the nutplates to the fuselage flange where the cowl met and used a similar technique.
15) At this point I did not install the left and right nutplates where the top and bottom halves of the cowling connect to the fuselage.

Tuesday, September 08, 2009


Some major steps have been taking with the wiring, with a bunch of "lessons learned".

The approach I took was what seemed logical to my programmer mind. I took a look at each device, the inputs and the outputs and made a series of sub harnesses. Connectors ( D-Sub 9 ) are used where two harnesses would need to join together.

Rough distances were measured with approximate routing.

Each sub harness was made in relative isolation.

This worked fairly well. Some of the earlier harnesses are a little untidy. None of them match in size.

As I went to install the harnesses this weekend I realized that I needed more of an "integrative" approach to the wiring problem. Lots of single wires got tangled up with each other. Wires drooped all over. The whole thing was a rat's nest mess.

I took everything back apart. Slowly I added one sub-harness back in at a time. With each new addition I attempted to clean up the harness and wrapped the wires into more logical bundles.

As the harness was put in, those bundles were bundled with the other bundles. The ground terminals were grouped together and bundled. The power terminals for the two buses got a similar treatment.

While doing this the remaining amounts of wire were looped and tied off to further promote a clean installation.

I have a LED strobe with controller. The directions suggest placing the controller in the wingtip - but there is a problem. The controller has a built in fuse holder. To comply with FARs all fuses need to be replaceable easily, preferably in flight. So a bracket and mounting plate were made and installed on the passenger side. This plate extends from the bottom of the instrument panel to the "L" angle that runs along the passenger side to the firewall.

The strobe controller and buses were mounted to this.

A partial power up test was performed. The radio and lights were all working. The split bus was isolating and the terminal ground was fine. The trim indicator was working great and the trim rocker and joystick controls were all functional.

Tuesday, August 11, 2009


The pilot and passenger grips are now wired and ready.

For the FlightGrips you need to trim 1" off the factory Y grips, use a bushing to allow for the 1" shaft and drill a 7/32" hole for a bolt that secures everything.

The grips are very sturdy and use aviation grade heavy duty buttons and switches.

In my configuration the pilot and passenger both have PTT and Flip/Flop.

The pilot has a memory set button, elevator trim up/down and an intercom isolate switch.

Wiring the passenger grip was easy. The PTT and F/F are both on an off center trigger. Pull on the bottom is PTT, pulling top is F/F. It is very hard to accidentally pull the wrong trigger. FlightGrip's trigger is removable from the shaft. The grip is designed to open up down the center with the trigger being removable. There was plenty of room for the wires and some heat shrink.

The pilot's grip was harder. The trim and mem set switches are on the top of the stick. These buttons are mounted on a removable disk, making wiring easier. The pilot has the same PTT/FF button config as the passenger.

The passenger intercom isolation toggle is mounted as a thumb shaft on the grip. Accessing the connection points was much harder for this one.

To get the wires down the stick some scotch tape was used to secure the various bundles together and then shoved down. Fitting 15 wires down the shaft ( each in sub bundles by function & destination ) was a little tricky due to the narrow passage where the "Y" forms and the pivot point at the base of the stick.

Once the wires were out I closed the grips and bolted them onto the stick. Closing the passenger grip was easy. The pilot's grip had the problem of heat shrink and wires made inflexible by solder. Some bending and finessing had to be done to get the stick to close with wires routed around the holes for the mounting bolt.

Almost all the connectors I have been placing are DSub 9s. The originally intention was to use a DSub 15 for the pilot's grip and a 9 for the passenger. Instead the pilot's grip has two 9 pins. One connector has the PTT,FF,MemSet and isolation buttons. The PTT and FF's pins are in the same location on the passenger's grip. You could interchange the two connectors with the only side effect being to disable two buttons. This seemed like a more resiliant configuration and also lets me have the option of disabling the trim in the field if I need to.

To use both the rocker switch in the panel and the switch on the joystick a relay had to be used. Ray allen sells one for this purpose. In addition to the relay a small circuit had to be made. This multiplexes the two switches. When the relay is used what the switches are really doing is selecting what ground is being closed.

Two IN4001 diodes are placed in line to the joystick ( DPDT ). These are split from lines that go to the rocker. From the rocker and joystick each a line is sent to the ground.

Sunday, August 09, 2009





Wiring update:

Most of the wiring harness is complete. Lights, radio and utilities are done. The transponder, Dynon and alternator wiring remain.

To help reduce the clutter on the kitchen and workbench tables I started cutting the panel and installing parts.

Many months ago I mocked up my panel using lifesized print outs. This worked well, but many details were simply left out. Some of the parts of changed, and a few unexpected things have been added. There are more switches and breakers than I had planned for.

One challenge has been trying to plan around the throttle handle. The exact position of the throttle can not be determined with out the throttle bellcrank installed. Based on the expected position from other builders I have moved the Dynon more towards the centerline. I would prefer that the Dynon be centered with the pilot's seat, but that may be impossible.

When laying out there were a few factors I kept in mind.

1) Anything flight and emergency critical should be close to aircraft center. This is to allow the passenger access to the starter, ELT, ect.

2) Try to logically group switches by function

3) Keep power away from the primer.

4) Do not stack any switch above or below another.


I have also received my grips. The final choice was for FlightGrips ( no website ). These are a solid grip that bolt onto the Y stick.

Internally the switch poles are easy to access as the stick splits apart and the top cap is removable. You do need to be careful with how much heat shrink is used as to keep the wire flexible enough to route around the grip.

On the pilot's side there is a elevator trim up/down, PTT, Radio Flip/Flop, Radio Mem Set and intercom isolation.

On the passenger's side there is PTT and Radio flip/flop.

Wednesday, May 27, 2009

More wiring components have been ordered and the wiring is in full swing.

This week the full wire harness for the strobes and position lights were made including a strobe pattern selector.

The harness for the landing lights was also made.

The buses are in hand and ready.

A few questions still remain, like how to properly tie in the Ducati voltage regulator and the split master switch.

Saturday, May 02, 2009

Progress visually has been slow, but much has been done.

The majority of the effort has been spent researching the wiring portion of the project.

Recently I flew down to Oregon and purchased an ICOM A210, Garmin GX327 and an ELT along with the matching antennas.

I also have ordered the Dynon D180 Rotax probe package and many small parts for the wiring.

A wiring diagram has been made an is almost finished. It will get posted here for the benefit of others. This diagram was used to generate the parts list. It even goes as far to include the pinouts for each piece of avionics.

Recently the ignition key was figured out using a 12V latern battery. The strobe wiring was also confirmed.

Tonight the ICOM A210 had a temp harness made and was rigged to a headphones speaker and the latern battery to power it on. The faint sound of BFI's ATIS was able to come through without the antenna attached.

Monday, April 13, 2009

This weekend the engine mount was reinstalled. It was realized that there are two steel angles that have not been drilled into place yet and need to.

The next steps of the controls will require pulling the fuselage out to mount the rudder hinge. Foul weather prevented this. The hinges were fabricated over the weekend.

The wiring diagram was started. The current plan is:

Dynon D180
Airgizmo / Garmin 496
Garmin GTX 327 Transponder
ICOM A210 Transceiver

I am using Visio to create a fully detailed diagram. The hope is that I can decide on color coding before hand and decide where additional connectors may be wanted to help with maintainability.

Tuesday, April 07, 2009

I recently moved. Packing a mostly finished airframe and a "used" workshop and then moving it across town is harder than you would think.

First the plane with the gear was about two inches wider than the trailer. This required removing one wheel. Next there is the organizational issue. The new garage is smaller and needs more organization. The plane needs to sit at a diagonal to fit. Once the engine is hung the door from the garage into the house will need to be removed to fit the plane.

Recent progress has included mounting the rudder pedals, brakes and nose steering. I also fabricated the rudder cable pulleys and some rudder mounting parts.

Here is the new workspace ( Requires Silverlight )



Friday, February 13, 2009

This picture illustrates that I placed the horizontal stabilizer mounts 10mm to far inside on both sides.

Two options exist in my mind for fixing this.

The first option is to create a custom mount from the fuselage side shaped to clear the flange of the stabilizer's mount. This would require a spacer and a much longer bolt. It also increases the chance of the mount cracking.

The second option is to open the stabilizer and move the mounts 10mm outside. This may require some work to the spar.

The controls are coming along nicely. The push rods and flaperon bellcranks are all connected. The flaperon mixer is also connected. The pushrods terminate where they will exit the fuselage.

I also figured out the wiring for the strobes and nav lights. They were pretty easy to deal with, but finding a suitable location for the control unit may be tricky.

Thursday, January 08, 2009

I have been very bad about posting recently, but this should not be construed as the project not being worked on.

The whole workbench was partially redone and lowered about half a foot. This is so the plane can sit on its wheels on the ground.

The engine mount holes were drilled out to their final size and bolted on.

Work has started on the controls. All three bell cranks have been fabricated. The lower torque tube bearing was un-riveted to allow for the torque tube to be placed. I then found an unacceptable amount of ply, so a new lower bushing was fabricated to raise the torque tube up and remove the wiggle.

In addition I have fabricated the flaperon mixer bearings and started placing the "L" angle that supports them.

Tuesday, December 16, 2008



The front was buttoned up, the rear half of the engine mount was bolted on, the nose strut bolted on and the main gear were installed.

The plane is now rolling on its own.

Sunday, November 16, 2008

Another monster six hour session finished the drilling for the slats. Only a few "gotchas" were hit.

First with the trailing edge skin be careful with the holes of the ribs. The last hole for each rib intersected the skin. This normally would not be a big deal but the ribs were already riveted ( per instructions ) to the bottom half of the main skin. In two cases ( outboard skins ) there was enough edge distance to drill out the rivets and use a strap duplicator to carry the hole onto the edge skin. With my inboard skins I had to make notches for the rivet heads.

All four slat pieces are drilled to final hole sizes and are ready to be deburred, primed and riveted.

Saturday, November 15, 2008

First, to anyone who is about to order their wheels please, please, please pay attention. Just spend the extra $30 a wheel and buy the tubes. The Matco tubeless tires are a nightmare. Seriously, I would rather rivet my hand to a rabid raccoon than deal with those things again.

I probably spent 15 hours trying to get them to inflate.

Some of that time was spent trying to separate the wheels. They can be really tight a large amounts of brute force will need to be applied.

The valve stems are a pain to install. A local tire shop was kind and let me borrow a valve stem installer. After that you need to get the wheel somehow beaded with the tire AND then slip a crazy rubber band gasket on between the two halves of the wheel.

If you use the tubes then the valve just slips on through and the wheels self bead.


A huge amount of progress was made thanks to the help of another local 701 builder. Together we made substantial progress on the slats. The slats are pretty straight forward, except for a few gotchas that got me. The biggest has to do with the "L" angle that reinforces the slat skin near the supports.

Trying to be industrious I went and cut the "L", notched it, bent it to match and then located the holes and drilled them into one piece. I used one of the ribs to back drill into a mirrored rib and then duplicated the holes to all the ribs.

What I forgot to do was check that all the holes of the "L" went into the support. Luckily all the holes that made it into the support were within minimum edge distances, but one hole missed. So I had to drill a fifth hole into the "L" that then made it into the slat support.

In one monster eight hour session we got the "L" spar drilled into all four slat skins, all the ribs, supports and "L"s riveted together and on one piece the ribs drilled into the skin.

Sunday, November 02, 2008

Quick status update:

The doors are on, the latches installed, the hinges hinging.

The main gear have had their notches made and are test fit. The front fork is ready for the wheel and tire. The landing gear and strut fittings have finally been bolted into place.

I did have some problems with the Matco wheels. Despite following the drawing, I can not separate the front wheel halves. There does not seem to be a retainer clip or anything like it.







Sunday, October 05, 2008

The pilot side door is now installed along with the door handle and strike plate. The directions were lacking, and a backing plate needed to be made for the provided handle. I unscrewed the inside latch and measured the distance between the screw posts and the center piece.

After making the backing plates the handle was positioned using the backing plate and internal handle to determine where the strike plate needed to be.

The backing plate was then used as a template to drill into the fiberglass door and the handle as screwed together.

On the passenger side the door was thicker than the pilot side. This caused the screws not to reach through and thread into the door handle.

PROGRESS:
Controls ~2h ( 2h )
Fuselage ~251h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h, 2h, 5h, 6h, 3h, 5h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~510h

Sunday, September 28, 2008

The door problem has been resolve. the solution was to trim 20mm off the top edges of the door sills. The major issue was matching the already existing holes into the fuselage frame. This was achieved by using a strap duplicator and the trimmed section of metal itself.

Once that was done, the hinges were drilled into the top of the door frame, then the hing was drilled into the door at some key spots to make sure the holes would clear.

After that one of the Dremels was revived with new motor brushes and the doors marked and trimmed.

PROGRESS:
Controls ~2h ( 2h )
Fuselage ~243h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h, 2h, 5h, 6h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~502h

Tuesday, August 26, 2008

Detailed photos of the bubble door fit problems I am having.

Sunday, August 24, 2008

It has been a while since the log has been updated, but that is not to say progress has not been made.

The roof has been drilled into place. The doors have been test fitted, and problems have been found. The windshield is sitting in place. The front landing gear is not being worked on.

PROGRESS:
Controls ~2h ( 2h )
Fuselage ~237h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h, 2h, 5h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~496h

Tuesday, July 22, 2008

Three hours were spent trimming the door sills and getting them drilled into place on the outside.

I decided to modify the trimming on the inside rear. Having the flap of aluminum that goes up next to the wing mount seemed wrong. It could not have provided any strength to the hinge mounting below, it made installation a pain in the ass, it would be hard to reach for riveting and it obscures an inspection point. Given that, I just lopped it off.

PROGRESS:
Fuselage ~232h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h, 2h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~489h
I spent about two hours trying to figure out how to trim the door sill ( 7F19-12 ).

The plans and directions are very lacking about the door sills. The forward half of the sill is easy to figure out, the outside rear is strange ( but figure-out-able ), but the rear inside is an enigma.

A quick search of the Matronics list and Google provided nothing.

PROGRESS:
Fuselage ~229h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h, 2h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~486h

Wednesday, July 16, 2008

Arlington 2008 Flyin:

It has been a while since the worklog has been updated, but progress has not totally stalled.

About six hours of work have gotten snuck into the project between life and Arlington.

The firewall has been fully clean, protected, reassembled and riveted together. In addition all the forward fuselage parts have been clecoed back together.

Some amount of time has been spent enlarging holes, finding missed holes, ect.

The next order of business are the doors. The directions are skimpier on these parts, so inferences need to be made. One issue is the existing holes that join the V-brace with the aluminum tubing along the top. The door sill sits on top of the tube, and it is impossible to back drill from the tube side. After talking to Zenith it is acceptable to 1) Use a strap duplicator to find the holes OR 2) Trim the door sill in such a way that these holes are bypassed.

Also I received clarification on the install order. 1) Doors 2) Skylight 3) Windshield.

PROGRESS:
Fuselage ~227h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h, 6h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~486h

Sunday, June 22, 2008

I spent about two hours Sunday cleaning up most of the firewall and then applying corrosion protections. The landing fork section still needs to be drilled to size.

One major problem is the lack of A5 clecos. Make sure you have at least 100 of them.

PROGRESS:
Fuselage ~221h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h, 2h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~480h
I have finally started drilling out the holes in the firewall. These have been A3 size since the initial assembly just in case I needed to adjust something when working on the rest of the fuselage.

Today I noticed a small amount of corrosion around one of the clecos on the firewall, so it was decided to drill everything out, deburr, acid etch, scotchbrite and then zinc as soon as possible.

All of the holes ( save the engine mount bolt holes ) that lay in the horizontal plane are drilled.

PROGRESS:
Fuselage ~219h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~478h

Tuesday, June 03, 2008

The color of the clecos on the nose skins have been changed from silver to copper.

PROGRESS:
Fuselage ~216h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h, 1h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~478h

Sunday, May 11, 2008

Saturday brought another two hours of work on the dashboard.

The upper ( "L" ) angle was drilled into place. The lower rivet lines of the top skin were also drilled into place.

In addition the top skin was trimmed per the plans.

After getting some unexpected time off, I have decided to fly the 150 to Oshkosh this year. The preliminary planning has started. It will be a long flight in the 150 as it cruises at only about 85MPH... about the same speed as the 701!

PROGRESS:
Fuselage ~215h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 2h, 3h, 2h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~477h

Monday, May 05, 2008

A quick update -

It has been rare to find time into the garage but progress has been made. The top nose skin is now drilled into place along with the ("L") angles that line the tops of the side skins.

Sunday, April 06, 2008

Saturday night saw three hours of progress.

The first draft of layout for the instrument panel was done. I found various pictures of the planed instruments and then printed them out at actual size. Some items got a hand drawn picture as a placeholder. A single piece of tape was used for each "instrument" or "control" to hold it onto the panel. Everything is very easily repositioned.

The instrument plane's flange was also drilled in preparation for the dashboard, and a piece of ("L") was drilled into place that holds the instrument plane at equidistance from the firewall.

I laid out and cut 7F14-2 per the plans, and had to open up the holes to make it fit well. The holes extend too far forward and are too wide at the inside to be a perfect fit. A much better plan would have been to cut a template from cardboard THEN use that to make the real piece. In the end I am going to cover the dashboard anyway with upholstery, but anyone wanting to keep it as bare metal may want to take precautions.

The big issue of the night was with the instrument plane and some ("L") angle that runs from it forward. The basic idea of the piece is to be even along the top edge with 7F14-3, the forward side skin. The problem is that a crimp in the flange of the instrument plane would interfere with it.

The obvious solution seems to move the ("L") down ~10mm, but since 7F14-6R ( aluminum plate ) is already drilled into position, I can not trim the side skin to be even. Given the size of 7F14-4 ( top skin ) there may be enough play for it to not matter.



PROGRESS:
Fuselage ~211h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~473h

Sunday, March 30, 2008

Spent three hours working on the instrument panel.

The gussets that join the panel to the cabin frame were fabricated and drilled into place. The panel bottom channel ( 7F15-1 ) was also drilled into place.

First I would suggest drilling the channel into the panel first. This gives you a better idea of where the gussets should go.

Despite some careful initial fitting and measurement, the gussets ( 7F15-2 ) are a little further inside that I would like. By centering the panel channel first you can get a better idea of where the radius of the gusset should be.

Also you will have to trim the top of the gusset so it can clear the panel. The plans call for a line at 75mm up, but try making the line at ~100mm. Of course, your milage may vary.

PROGRESS:
Fuselage ~208h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h, 1h, 3h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~470h

Sunday, March 23, 2008



Got about an hour of work in. The ("Z") angle on the forward fuselage skin on the passenger side got measured, trimmed and drilled into place.

Once the initial rear hole is drilled into place and the position where it crosses the plate is determined, it is much easier to predrill the required holes into the channel, then drill into the fuselage skin.

The Rotax was finally uncrated ( mostly ). The shipping crate was secured in an unusual manner and required bending of metal to open. A quick inspection did not reveal anything missing or damaged.

PROGRESS:
Fuselage ~204h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h, 1h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~466h

Saturday, March 15, 2008

I spent about an hour on the fuselage. First we finished drilling the side skin extrusions into the nose skin, then we trimmed and drilled into place the upper ("Z") length that runs along the nose skin.

It turns out that the best way to approach the placement is to drill the aft most hole, then have a help hold the piece AND provide a buttress on the outside while you drill from the inside.

Also one of our EAA chapter members held a project visit today for their very nice looking 5151. Metal really dominates building so seeing how a wood project goes together was refreshing.

PROGRESS:
Fuselage ~203h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~465h

Saturday, March 08, 2008

Saturday was the first building session attempted since the birth.

I reconfirmed the positioning of 7F14-6 on the pilot and passenger side and then laid out the drill holes on the extrusion that extends from the fuselage sides.

Instead of drilling from the outside as was suggested by the HBH video, I ended up drilling from the inside to ensure edge distances.

At first I took a contortionist's approach by laying on the seats with my elbow resting on the floor pan, but I realized that I could simply sit on the edge of the workbench and lean in.

PROGRESS:
Fuselage ~203h ( 3h, 3h, 2h, 3h, 7h, 2h, 5h, 2h, 3h, 2h, 2h, 3h, 6h, 2h, 2h, 1.5h, 2.5h, 1h, 2h, 3h, 2h, 3h, 4h, 1h, 2h, 1h, 3h, 4h, 3h, 3h, 4h, 3h, 4h, 4h, 6h, 3h, 3h, 4h, 2h, 2h, 2h, 4h, 2h, 2h, 10h, 4h, 4h, 6h, 3h, 4h , 6h, 3h, 2h, 2h, 5h, 2h, 3h, 3h, 2h , 2h, 3h, 4h, 1h, 1h )
Wings: ~157.5h ( 1h, 1h, 0.5h, 2.5h, 4h, 1h, 1.5h, 1h, 1.5, 4.5, 1h, 1h, 2h, 4h, 1h, 3h, 1h, 2h, .5h, 1.5h, 2h, 2h, 2h, .5h, 1h, .5h, .5h, 2h,3h, 1h, 3h, 3h, 4h, 2h, 3h, 7h, 3h, 1h, 4h, 1h, 1h, 1h, 4h, 2h, 2h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 3h, 2h, 2h, 1h, 2h, 3h, 2h, 1h, 1h, 1.5, 2h, 2h, 3h, 2h, 1h, 3h, 2h, 1h, 2h, 1h, 5h, 2h, 1h, 2h, 4h, 2h, 3h, 3h, 3h )
Flaperons: ( DONE! ) 23.5 hours spent ( 3h, 1h, 1h, 1h, 1.5h, 3h, 6h, 3h, 4h, 1h )
Paint Design: 2 hours spent ( 1h, 1h )
Elevator DONE!: ~31.5 hours spent ( 3h, 1.5h, 3h, .5h, 3.5h, 2h, 4h, 1.5h, 2h, 4.5h, 1h, 6h )
Horizontal Stabilizer DONE!: ~28 hours spent, 3 pieces replaced ( 3h, 2h, 2h, 2h, .5h, 1.5h, 3.5h, 1.5h, 5, 4.5, 2h, .5h )
Rudder DONE!, minus horn : ~16 hours spent, ( ~8h, ~8h )
-----------------------
Total Done: ~465h

Friday, March 07, 2008

We just had another delivery today. Only this baby eats premium gasoline, is Austrian, makes 100hp instead of diapers, and weighs 160lbs.

Tuesday, March 04, 2008

So it will be some time before the plane gets worked on again. My wife just finished a nine month long project, and we just started a project that will take a minimum of 18 years...



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